AJp80 Posted February 28, 2018 Author Report Share Posted February 28, 2018 It has been quite a while since I’ve updated this thread. I’ve been consumed with wrenching and chasing down problems instead of writing about them. I’d like to keep this thread updated and keep the story going. In the last year, I manual swapped the car and did a lot of interior work. On the night that I got my parts car, I dropped a wrench on the MAF and poked a hole in it. Years ago, my grandpa fixed a hole in water heater by covering it with a penny. The penny held things together until after my grandma sold the house. Continuing in that tradition, I saw that the little hole I made on the MAF was a little smaller than a penny. Problem solved. Pre-manual swap: I got my s70 out to some local shows and the crowd went mild (feat. @babyclaude)! 2 Quote Link to comment Share on other sites More sharing options...
gdog Posted February 28, 2018 Report Share Posted February 28, 2018 2 hours ago, AJp80 said: On the night that I got my parts car, I dropped a wrench on the MAF and poked a hole in it. Years ago, my grandpa fixed a hole in water heater by covering it with a penny. The penny held things together until after my grandma sold the house. Continuing in that tradition, I saw that the little hole I made on the MAF was a little smaller than a penny. Problem solved. Grandpa must be smiling.. Quote Link to comment Share on other sites More sharing options...
AJp80 Posted March 1, 2018 Author Report Share Posted March 1, 2018 Leading up to the manual swap, I replaced a wheel bearing. I didn't pick up on the change in size from E16 on the 850 to E14 on the S70 and stripped the head of the screw. Using a cutoff wheel, I reshaped the head of the screw until I was able to get it out using a lot of heat and an adjustable wrench or vice grips (I forget which). This victory of man over bolt was another proud moment for me. 1 Quote Link to comment Share on other sites More sharing options...
AJp80 Posted March 1, 2018 Author Report Share Posted March 1, 2018 (edited) Manual swap goodies! Resurfaced SMF flywheel, 850R clutch, Kaplhenke Delrin subframe bushings, an OBX ehaust, AEM UEGO wideband and a japanifold that is still to be installed. Again, tons of help to @andyb5, @babyclaude, and @huntec for their time and patience with this swap. Thanks also to @Leco510for lending me a flywheel. Here’s the donor car with a warped head that I got for free. All I needed to do was tow it off the top of a mountain. Thanks again to the unstoppable Andy for going on a towing adventure with me. I had to move for work before I could fix the wagon, so she donated her transmission to live on in my sedan. Springs, sunroof, and other parts found their way to my car or others in order to aid in this swap. Note the slammedness after I took out the rear springs. The front is on XC springs that were floating around the shop. fried head Chocolate shake Major surgery Those of you who are detail-oriented might have already spied the brown XC wagon outside the shop peeping at it's little brother being torn limb from limb on the lift. There's a great story behind that one for another day... Edited March 1, 2018 by AJp80 2 Quote Link to comment Share on other sites More sharing options...
AJp80 Posted March 1, 2018 Author Report Share Posted March 1, 2018 (edited) The p80 desk chair was another outgrowth of the sacrificial parts car. I gave the chair as part of the secret santa gift exchange. Luckily, the recipient donated the chair to the shop so I can still use it. I removed the seat skin, deployed the side airbag, and then repackaged the seat using zipties. Getting a decent pair of Channellock diagonal cutters made a huge difference when cutting through the hog rings. As always, the right tool for the job makes everything easier, and I was the right tool for this job. Due to the car being free, wood being $9, and me not caring about using nuts on every bolt, I was able to come in well under the $20 limit. I didn't want to make it too nice though, so the seat is all the way back on the rails and any amount of lean leads to Virtucon levels of tilt. Edited March 2, 2018 by AJp80 1 Quote Link to comment Share on other sites More sharing options...
AJp80 Posted March 2, 2018 Author Report Share Posted March 2, 2018 (edited) Enough teasing, on to the good stuff! The manual swap begins! Here's the engine and trans out of the car. I eventually went back and redid the conduit on those injector wires. Another broken bolt, this time it was a stud in my turbine housing. I drilled this out and replaced it with a nut and bolt. Not ideal, but working. This broken stud is what deterred me from trying to do the japanifold during the manual swap. After dealing with that setback, I separated the transmission and got to work with the flywheel, pressure plate, and clutch. That's me sitting on my automatic while installing my M56 and torquing down the bellhousing bolts with my S70 winking at the camera. I'm lucky to have a girlfriend who was nice enough to bring me meals and pass me bolts in the shop. Delrin subframe bushings for the win!! They were incredibly tough to seat, but I got most of them in with a hammer. That being said.... eventually, disaster struck! While installing a subframe bushing, I tried to seat it by tightening the bolt into the subframe. Working late into the night, I borrowed an electric impact, set that puppy to full power and promptly sheared the bolt in two! I let loose my loudest F-bomb, and took a damn break for the night. Sometimes, nothing good happens after midnight. When I got back in the morning to survey the damage, I saw that the bolt had actually broken off inside the alignment tab....not good... Broken bolt (head side): Here, you can see the broken bolt inside the subframe... Most of the threads of the bolt were stuck inside the alignment tab Edited March 2, 2018 by AJp80 1 Quote Link to comment Share on other sites More sharing options...
AJp80 Posted March 16, 2018 Author Report Share Posted March 16, 2018 (edited) Long story short, I was able to get the bolt out by grabbing at the three shear failure points with angled long nose pliers and gingerly twisting them for about 20 minutes. At the end of the day, I finally got it started. https://i.imgur.com/IWaqQuL.mp4 Funny thing... the second time I started it up, it ran fine but the power wire on the starter rotated when I shut off the engine. This caused the power wire to touch to the control wire and make the engine turn over continuously until I could find a 10mm socket to disconnect the battery. I also replaced my ratty old steering wheel with a wood steering wheel.... might be a bit crooked. I fixed that later. You can see my wideband gauge in the vent too! Got a tune from Aaron to account for the downpipe and turn up the boost! Gotta love a big red button. I got a tip that a chair leg tip seals off my deleted PCV inlet nicely. When I did a few pulls for datalogging, I blew off an intercooler hose going uphill in the dark... that was alarming.. After the manual swap, I got down to finally putting in the headliner that I reupholstered when replacing my sunroof. Many many thanks to @babyclaude for shepherding me through this process. I took three trips to fabric store to get the right look. I went with a pattern called "Pearl Gray Bernegat Plaid". I did this over the summer and finally reinstalled it in December. Edited March 16, 2018 by AJp80 1 Quote Link to comment Share on other sites More sharing options...
AJp80 Posted March 16, 2018 Author Report Share Posted March 16, 2018 I gave my window control buttons some TLC. I used Pledge to clean the gunk off my buttons, and the results were incredible. Left is untreated and right is cleaned up. I got the left one looking more like the right one after this picture. The white parts where bits of paint are worn off the buttons are from me using Goo Gone. I took the shells apart and sprayed the contacts with some CRC Quick Dry contact cleaner and now my rear passenger window works! I think the top one is the treated one. I did the same thing with my seat controls (and all my spares). Now my all my seat adjustments work too! I really like this CRC stuff. 1 Quote Link to comment Share on other sites More sharing options...
gmsgltr Posted March 16, 2018 Report Share Posted March 16, 2018 nice work Quote Link to comment Share on other sites More sharing options...
apeacock Posted March 16, 2018 Report Share Posted March 16, 2018 Rensselaer is the secret NY hub of volvo mods. 2 Quote Link to comment Share on other sites More sharing options...
AJp80 Posted March 16, 2018 Author Report Share Posted March 16, 2018 1 hour ago, apeacock said: Rensselaer is the secret NY hub of volvo mods. RPI is where old Volvos go to get their guts ripped out and swapped around. Quote Link to comment Share on other sites More sharing options...
apeacock Posted March 16, 2018 Report Share Posted March 16, 2018 3 hours ago, AJp80 said: RPI is where old Volvos go to get their guts ripped out and swapped around. Hey I've done it there too, I know! I should come back again. @andyb5 I really want to drop my rear frame and refit the fuel system. Quote Link to comment Share on other sites More sharing options...
andyb5 Posted March 17, 2018 Report Share Posted March 17, 2018 8 hours ago, apeacock said: Hey I've done it there too, I know! I should come back again. @andyb5 I really want to drop my rear frame and refit the fuel system. Ugh. That job is such a bastard because of all the things that can potentially go wrong. Quote Link to comment Share on other sites More sharing options...
AJp80 Posted April 24, 2018 Author Report Share Posted April 24, 2018 (edited) I FINALLY fixed my cruise control. It's been broken since the the manual swap. I couldn't figure out what was wrong until I used a hand vacuum pump and tested the vacuum at the pedals and under the tray. It turns out that I accidentally unplugged the vacuum line from the pump to the pedals during disassembly. In the photo below, you can see the empty port. Earlier on, I thought it was an used for something else on the donor car so I plugged it. once I got it all together, cruise worked like a charm. Maybe this will be useful to others. It seems like no cruise after the manual swap is a common problem. In other news, I'm taking a bit of a break from working on my car so I can focus on getting out of grad school. I'll update with small weekend projects here and there, but nothing big until August. Edited April 24, 2018 by AJp80 Quote Link to comment Share on other sites More sharing options...
sventastic Posted April 24, 2018 Report Share Posted April 24, 2018 Photo doesn't work unfortunately. Would be useful though, I'm doing this swap this week! Quote Link to comment Share on other sites More sharing options...
Recommended Posts
Join the conversation
You can post now and register later. If you have an account, sign in now to post with your account.